The output value of discrete PID controller is NaN

11 Ansichten (letzte 30 Tage)
lim daehee
lim daehee am 19 Mai 2020
Kommentiert: Zheng Zhang am 8 Sep. 2023
I'm trying to control motors with pwm signals.
when I clicked monitor & tune button, I found some outputs of discrete PID controller block is NaN. It is stated below.
Other input from same bus, yawspeed, generate normal value, however, pitch and roll angles have nan value.
I first thought that the problem is from the difference of data type.. so I checked data types of all inputs and outputs and there are no problems with data types.
Is there anyone who know why the nan value is generated?
  2 Kommentare
Ameer Hamza
Ameer Hamza am 19 Mai 2020
Try to monitor the input of PID blocks. Are the input values finite?
lim daehee
lim daehee am 19 Mai 2020
Nope, I monitored all values including input of PID blocks, however, they are all not inf or nan and it ranges from -0.02~0.02
The output saturation is limited from -0.1~0.1.
Additionally, I changed inputs(pitch_angle, roll_angle)into constant block with a constant value and the model works fine.
However, when inputs are from uORB block, the output of PID block has nan valeu.

Melden Sie sich an, um zu kommentieren.

Antworten (3)

Ankur Bose
Ankur Bose am 28 Sep. 2021
Answered the same question here
https://www.mathworks.com/matlabcentral/answers/527384-i-gain-of-pid-controller-has-nan-value-simulink
  2 Kommentare
勇刚 张
勇刚 张 am 19 Mai 2022
This method can solve the problem
  1. Ensure that initial inputs are not NaN. in PX4 thing might happen when you are trying to read from vehicle attitude connected to rotation block. Initially the estimator might not have started which caues attitude not to be published and hence uORB block retutns [0 0 0 0] as quat which are invalid and hence rotation block computes NaN and passes to PID. Eventually this might be fixed but PID will still store NaN.
  2. Reset the PID block using and external signal when values are stored
Zheng Zhang
Zheng Zhang am 8 Sep. 2023
您好,能详细说一下您是怎么解决的吗?

Melden Sie sich an, um zu kommentieren.


Jonas
Jonas am 19 Mai 2020
Check the block 'Rotation Order: ZYX'. Does it work properly?
  1 Kommentar
lim daehee
lim daehee am 19 Mai 2020
Bearbeitet: lim daehee am 19 Mai 2020
I changed pid controller into p controller and it works fine. So I think rotation order worked well. Also, I think d and i controller is the problem, but I don't know why d and i gain caused the problem.

Melden Sie sich an, um zu kommentieren.


Kunal Lad
Kunal Lad am 31 Jul. 2020
Hey Lim Daehee,
Did you find the solution to this problem as I am facing it too. Share up if possible.
Thanks.

Produkte

Community Treasure Hunt

Find the treasures in MATLAB Central and discover how the community can help you!

Start Hunting!

Translated by