How to reduce overshoot of output response in BLDC motor?

3 Ansichten (letzte 30 Tage)
melinda fauziah
melinda fauziah am 18 Jan. 2017
Hi everyone, I have a problem in my project. It's about Fuzzy Gain Scheduling of PID controller for BLDC motor. I’ve done with Simulink simulation. But the output response still not good. The overshoot came when I change the set value. I attach the result on the link below. I hope someone can give me the suggestion what I have to do. Thanks a lot.

Antworten (1)

Arkadiy Turevskiy
Arkadiy Turevskiy am 19 Jan. 2017
Look at the control request your controller is generating. The type of response you are getting might be due to the fact that the controller output is limited, but the integrator in the PID controller "winds up" and take a while to unwind. You may want to try using anti-windup in your controller.

Communitys

Weitere Antworten in  Power Electronics Control

Kategorien

Mehr zu Fuzzy Logic Toolbox finden Sie in Help Center und File Exchange

Community Treasure Hunt

Find the treasures in MATLAB Central and discover how the community can help you!

Start Hunting!

Translated by